The 350 was originally a 2 bbl, almost 20 years ago I put in a Qjet(17054913), cast iron intake manifold, timing set, and 067 cam. EGR, heat riser valve, and thermal vacuum switch are not hooked up. Distributor vacuum advance connected to ported source. 18" vacuum at idle. 14 degrees timing.
I did not try DB rods but I have a set I can try.
Trans kickdown was not working and I thought I read somewhere about tuning secondary with kickdown disabled. I cleaned and adjusted the kickdown switch and it works now.
I sent the carb baseplate to you for rebuild and bought a SR rebuild kit. I converted to electric choke, vacuum passage blocked off. Drilled base for .080 idle bypass, 73 jets, 44 rods, idle tubes .038, idle down channel .050, Lower idle air bleed .067, upper IAB in main body .067.
Main air bleed in main body was .055, I drilled out to .067. Main air bleed in air horn is .070. Secondary air flap cam and spring replaced and adjusted to 1/2 turn past closing. Air flap opening is 1.350". Secondary air bleed tube was.032, I drilled out to .036. Float replaced and set at .25". APT adjusted to 2.5 turns out. Choke pulloff replaced. That's about it.