Made sure both sides were open from baseplate to airhorn.
Opened up the bypass air (both sides) from .070 to .113, going .010 at a time in 4 steps and then testing idle functions at each step/increase. If I turn the screws in all the way vacuum drops and gets more erratic and it idles rougher but still can't kill it with the screws. At 1 turn out on both sides it idles smoother than before, and part throttle is much crisper, stronger and not 'jerky' when cruising. If I remove my vacuum gauge to create a leak the RPMs still increase, but not as much as previously.
New development though. On my test drive, WOT just isn't working, as if it's choking out all the way to redline. Maybe need to loosen my air door spring? I believe it's around 1 turn in. WOT was the only 'part' of the carb I had dialed in before!