I haven't replaced the inline filter. It flows fine once flow is established. I could replace it though, it's a cheap thing to try.
Float position didn't match what was called for in the table I referenced. That's why I adjusted it.
It was rebuilt around 2000 miles ago per the previous owner. Appearance of gaskets and other internal parts would support that. I bought an over the shelf kit but just used the gaskets, still have the rest. I realize I should've bought Cliffs kit but was in a hurry. I'm in the middle of Cruisin' the Coast.
If the bowl plugs aren't leaking (they aren't) why is the bowl empty in the morning? Only one other place for the fuel to go, right? Back the way it came, toward the fuel pump.