The fuel pump pushrod was 1/2 shorter than stock, so I replaced it. I ended up pulling the carb apart. Checked the needle and seat size, it was .120, too small! I installed a .135 from Cliff and have no more sag at full throttle. Still using the GM mechanical pump and not the electric intank conversion I was considering.
People check that needle and seat, it makes a big difference.
Thanks Cliff!