Cliff and Kenth,
Thanks guys for stickin' with me through this.
I couldn't leave well enough alone. Engine seemed like it wanted a bit more fuel, so I tried to figure out why it was running well at:
IT .031
UIAB .042
DCR .047
IABP .052
Jets .074
Rods 50C
First off, remember that this engine has a roller cam and short piston skirts. It also has a crazy tight 109 center cam (19.5 in Hg), vortec heads and moderate compression (9.1:1). Put this all together, and it is more efficient than most.
If Cliff will recall from our phone convo a year ago, I originally used the .036 jets, but couldn't get it to idle down until I blocked the IABP. This is when I was using the bore UIAB at .070. I also had high sensitivity to engine run-on after the key was turned off. Engine run-on typically means too much fuel in the motor after shut-off. That's why I killed it back with a .031" idle tube.
I ran some calculations on fuel through an orifice and found vacuum of 19.5 in Hg through a .031 idle tube, pulls the same as 16 in Hg through a .033 tube.
I then looked at the ratio of air to fuel between the UIAB and IT with my current IT .031, UIAB .042. Keeping the ratio the same, I extrapolated the following table:
1.75-1.85
IT (in) UIAB Rec UIAB Rec (mm) Input Actual UIAB Rec UIAB/IT Actual UIAB/IT
0.031 0.042 1.07 0.042 1.84 1.84
0.032 0.043 1.10 0.043 1.84 1.81
0.033 0.045 1.14 0.043 1.84 1.70
0.034 0.046 1.17 0.047 1.84 1.91
0.035 0.047 1.20 0.047 1.84 1.80
0.036 0.049 1.24 0.047 1.84 1.70
0.037 0.050 1.27 0.052 1.84 1.98
0.038 0.051 1.31 0.052 1.84 1.87
Thing is, you only have a few sizes in a numbered drill set to achieve the orifices. So, you gotta choose what is closest and hope for the best. That is what "actual" indicates. The actual drill bit you have in your index.
Being that the idle screw was just barely off the stop at IABP .052, I decided to choke out some bypass air to reduce my idle and allow better use of the idle screw. I choked it back to the next drill bit, .047".
I also thought it wouldn't hurt to run the float a bit lower than my tested and true 3/8. So I put it at 7/16. With a .135 needle seat orifice, I should never have a float issue. Obviously, I don't plan to go racing. 4500 rpm is my shift point.
So my new calibration is:
IT .032 to .0325
UIAB .043
DCR .047
IABP .047
Jets .074
Rods 50C
APT 2.5 (still does not go lean with a quick hand over the airhorn)
Float 7/16
Note that idle mix screws are 3.0 turns out. It actually works at 2.5, but I can eliminate the pip, pip, pip form the exhaust with another 1/2 turn.
I think your single taper 50C rods will optimize gas mileage. But, I do like the double taper 50M because once it hits the second taper, it comes alive well before full throttle. However, if you are pulling a trailer and the piston rises to this level, you will surely consume more gas than with the single taper.