429bbf,
Checked float level, was 9/32, changed it to 13/32 as spec'd in rebuild sheet.
Disassembled seat and checked gasket and mating surfaces. All looked good reassembled.
I don't have the degrading idle anymore. Your excellent advise on checking float level helped.
Von,
Secondary to primary rod was OK as I mentioned before, so I plugged the .081 Air bleeds.
I also checked the the vac advance and the choke pull-off. Both held vac without leaking down.
I also backed off on the choke fast idle screw, it wasn't touching, made no difference.
So now I can get it to idle down to 680-700 with pvc attached and vac advance attached to manifold vac. Idles very nice and smooth. If I slowly work the Idle mixture screws in it won't reduce idle, just degrades it till the engine runs rough and dies. I can back the idle adjustment screw on the throttle blades all the way out and the slowest idle I get is 680-700.
If I pull the PVC it will idle down to like 550 or maybe even less. If I pull the vac advance and plug or switch it to the ported vac source I can get the idle down. But the idle is rougher.
The timing is set at a total of 34 deg all in. Intial timing is 12 btc. When at Idle with vac advance on man. vac I get about 24 total at the 680-700 idle.
I'd like to get the idle down to about 600-625. I can do it with no PVC or ported vac for the dist advance but then the idle is rougher. Seems like idle is lower cause the engine is struggling. Maybe I should work on getting a better idle quality using the ported vac. At 680-700 with vac advance on man vac and pvc attached the idle is silky smooth. I'd just like to knock it down about 75 rpm's.
Von, I think your suggestion of plugging the air bleeds helped knock the idle back about 100 rpm's. Thanks!!
Anymore ideas to help me over the hump?
Thanks both Von and 429bbf for your help so far!!