Yes, it had a plug in the throttle body. I removed that back in 1980, and "adjusted' it LOL.
We did get this fired up today. Ran it @ 2500 to break-in the valve train. When I closed off the airhorn with my hand it did pick up RPM. So at least the part throttle is on the lean side.
Still have to get it set to road test. The idle seemed kinda rough, will play around with initial timing/ vacuum advance. It does not seem to like manifold vacuum or 13* in the can is too much.
I looked at the hanger and metering rods, yea they are not stock...Must have 'adjusted that' too.