Edelbrock 1903 to be used on HT383, 9.1:1 static, 196/206 .431/.451 109, 10 initial + 22 mech @3k.
Calibration as purchased used, but never ran on this engine. Note this carb was all black inside. Was running rich!
Hot Air Choke
Needle Seat .130
Float 7/16
IT .033
UIAB .070 (in body)
DCR .055
LIAB .064
IDP .084
IABP .052
SMAB .052 (in horn)
Jet .073
Primary Rod 50M
APT Spring Silver
Acl Well .040
2ndy Rod DR
2ndy Hanger S
2ndy Bleed Tube .026
2ndy DP .052
Choke Pull Off 2.5
2ndy Spring 7/8
Second calibration per Cliff. I could not get this to idle down until I plugged the IABP. However, it still ran on even on 91 octane. Pull off vac hose and idle goes up. Zero response to APT tip-in procedure. No hesitation off-idle or thru 2ndy. Engine tries to die when let off throttle to complete stop. Electric choke works fine, but loads up.
Electric Choke
Needle Seat .156
Float 7/16
IT .036
UIAB .070 (in body)
DCR .055
LIAB .064
IDP .089
IABP Plugged
SMAB .052 (in horn)
Jet .074
Primary Rod 50C (Cliff custom full taper)
APT Spring DkBlu
Acl Well .040
2ndy Rod AX
2ndy Hanger S
2ndy Bleed Tube .026
2ndy DP .052
Choke Pull Off 2.5
2ndy Spring 7/8
3rd Calibration. Leaned it out, trying to kill the run-on and overly rich condition. Bushed primary shaft. Idle screws 4.0 turns out and turning in kills engine, bad off-idle stumble in cold weather (have to flutter acl pump), no engine run-on, pulling vac hose increases idle, zero response to APT tip-in procedure, choke works
New Primary Shaft Bushings
New Needle & Seat .135 <-Found tool chatter in the larger seat
New Float <- Old and new both weighed 6.5g, but new had heel farther away from fulcrum
Float 7/16
IT .031
UIAB .041 (moved to horn 6-32 setscrew, plugged old with sinker lead)
DCR .047 (8-32 setscrew)
LIAB .064
IDP .089
IABP plugged
SMAB .052 (in horn)
Jet .074
Primary Rod 50C (Cliff custom full taper)
APT Spring DkBlu
Acl Well .040
2ndy Rod AX
2ndy Hanger S
2ndy Bleed Tube .026
2ndy DP .052
Choke Pull Off 2.5
2ndy Spring 7/8
4th Calibration. Opened IABP since idle seemed to want air when removing vac hose. Idle screws 3.5 turns out and turning in kills engine, bad off-idle stumble in cold weather (have to flutter acl pump), pulling vac hose increases idle, zero response to APT tip-in procedure, choke runs rough
Seat .135
Float 7/16
IT .031
UIAB .041 (moved to horn 6-32 setscrew, plugged old with sinker lead)
DCR .047 (8-32 setscrew)
LIAB .064
IDP .089
IABP .052
SMAB .052 (in horn)
Jet .074
Primary Rod 50C (Cliff custom full taper)
APT Spring DkBlu
Acl Well .040
2ndy Rod AX
2ndy Hanger S
2ndy Bleed Tube .026
2ndy DP .052
Choke Pull Off 2.5
2ndy Spring 7/8
5th Calibration
Pulled the 1903 off and replaced with a junk 70 series from a 350 truck. Runs fine, but no choke (I have vortec heads). Surprised how much quieter the exhaust is with this carb. No run-on, no stumble, no dying when quickly decelerating to a stop. Pretty good for an old junk carb.
Got to say, I've spent way too much time and money on this thing. Pretty frustrated. Can anyone see where I've gone wrong? Never had this much "fun" with a quad before.
I'm scared to go back to a bigger idle tube, since it already seems rich regardless of what I do. Setting the float to 9/32" doesn't seem like it would help. Why is this not responding to the APT Tip-in?