I've heard many times of folks curing fuel delivery issues by removing the stock fuel filter and installing an in-line filter. The theory sounds great and it gets regurgitated frequently on many websites when the topic comes up related to using a Quadrajet in a "high performance" scenario.
So I took my car to a local test and tune session and did some testing.
When drag racing I used an 8AN line from the regulator (mounted at the front of the drivers side valve cover) to the carburetor. The fuel filter is a high flow racing type unit mounted behind the tank next to the 140gph fuel pump.
Never one single issue with fuel delivery with this system.
So to test the capabilities of a stock paper filter put a 3/8NPT to 3/8" steel fuel line adapter in the regulator and ran a 3/8" rubber hose to the carbs stock fuel filter housing with a paper filter inside.
I had already rigged this up and made two passes before installing it to replace the 8AN set-up.
I made three more track runs, two are shown below, the first one is before the change and the second one after the change 23 minutes later:
R/T: .505 .514
60': 1.6230 1.6289
ET: 7.3169 7.3188
MPH: 94.35 94.36
These are 1/8th mile ET and MPH. You'll notice that my daily driven street car is a little faster than most so fuel consumption on a run, and acceleration trying to put fuel back in the tank would be a little more taxing on the system than most set-ups.
I think this pretty much proves that fuel delivery to the nose of the carburetor is far more important than what filter you have in line on the pressure side of the system. As long as it's not clogged up the factory paper filter used in a Q-jet certainly appears to be more than adequate to support big HP levels and pretty quick vehicle performance......FWIW.....Cliff
PS: some folks may notice that it actually ran slightly quicker after the stock filter and smaller feed line from the regulator was installed. This is going to be due to a very slight improvement in weather conditions as it was done in the evening and things were cooling off pretty quickly that night.